With the gearbox/clutch issue sorted, it was time to get commissioning, starting by chucking the batter on charge for the duration and the earth cable from the front earth mount to the gearbox and gearbox to battery cables added to the earthing point on the gearbox...

… but the bolt looked a bit past it, so this was replaced with a new alternative. The battery charger was then attached for the duration, to ensure it was ready to go.
From there I started with the bevel box, the oil for which I had already got, FUCHS 80W-90 gear oil.
The drain plug torque was checked and the filler cap removed to allow the oil to be added up to the bottom of the threads of the filler, using about 260ml...

… the bevel box was rotated, with the gearbox in neutral, and the level checked before the filler cap replaced and torqued up. It's worth mentioning here that I cut a slot out of the funnel I use to allow the end to be drawn round on itself and fit into the smaller filler hold on the bevel box.
For the gearbox oil, the drain plug torque was checked, filler removed and the same FUCHS 80W-90 gear oil was used, using about 875ml of oil to reach the mark on the dipstick (tool kit C-spanner)...

… the gearbox rotated and run through the gears while rotating the back wheel by hand. The level was checked again and the cap fitted and torqued down.
And moving forward, it was time for engine oil, deciding to go with FUCHS Semi-Synthetic 10W-40 as it gave the greatest temperature window for operation across the temperatures usually seen in the UK.
As before, the drain plug torque was checked, the filler cap removed and the oil poured in to a good volume in the sump and the engine turned by hand before topping up again and replacing the filler cap replaced.
The spark plugs were next in line, these were taken out, cleaned up with a wire brush and the gap checked with a feeler gauge to ensure they are within service tolerance before refitting and the HT leads reattached.
I managed to get myself a replacement sticker for the coil pack, so I removed the cover for the coils to expose the damaged sticker cleaned up the coil and fitted the new sticker...

… unfortunately not a match, but it conveys the warning it needs to!
So, moving onto the rear brake, everything was wrapped in rags to protect it from brake fluid the reservoir was topped up, clear tube and pot connected to the nipple and the bleeding began from the ABS Pump, slightly applying the rear brake, opening the bleed nipple, pushing the foot brake through it's travel, closing the blood nipple and releasing the rear brake - bleeding the ABS pump before moving onto the rear caliper and repeating the operation.
Despite the bleeding, no brake pressure, so I repeated the bleeding process, and there was more air. As I got frustrated I shelved it for now and started on the front brakes - I'll come back to this once I've given it some thought.
The front brake reservoir was topped up and the brake lever tied up with an elastic band the nipple on the ABS pump was opened and allowed to gravity bleed (mainly so I could have a coffee!), this was repeated with the nipple on the left front caliper...

... and the bleed was done, pumped the brakes a few times and all the pads moved - so job done, or so I thought.
There was a puddle of brake fluid, I traced the leak back to the front brake master cylinder so the front brake reservoir was emptied, and the mess cleared up. I was somewhat disappointing as this was working perfectly before the strip down, maybe it was time for this to fail, maybe it just needs a good clean.
The front master cylinder was disassembled and cleaned before being reassembled and the unit held with the plunger up and a small amount of brake fluid added - and I waited for any bubbles to indicate a leak ... nothing, happy is not the word.
The fluid was all cleaned up, the master cylinder remounted and the reservoir was topped up, with the system bled back through to clear any air...

... once everything looked clear of bubbles, the front brake was pumped hard again and tied back to allow any remaining bubble-shaped gremlins to work their way back into the reservoir over night. The next morning the brake was lovely and firm and ready to stop.
With the front done, it was time to head back to the rear brake, it was time to give the system a thorough check through. The right hand side footrest hanger was removed and the rear brake master cylinder unbolted and the master cylinder was dismantled and all the internal components were cleaned up...

... as well as the bore, to ensure a good fit. The back end of the master cylinder looked a bit cruddy so it was cleaned up with 600 grit wet and dry paper with a similar treatment given to the mating faces of the brake line. Once done, the banjo bolt was reinserted and wound to the stop, before being taken out 1 turn and the exposed bolt length measured...

... and the thickness of the brake line end measured, this meant I needed 2.88mm of washers just to make up the space, let alone the crush distance, so I put a stack together which measured 3.25mm and applied these to the bolt...

... wound the banjo bolt back in to hold everything together for now. The right hand side footrest hanger was bolted back in place and the same banjo bolt check conducted on each fitting, cleaning up and adding washers where needed.
Following that, each bleed nipple was taken out and checked for seating marks before each seat and nipple was cleaned up with blue roll to remove any contamination and refitted.
The brake fluid reservoir was topped up with fresh fluid and the gravity feed line pinched, just above the master cylinder to bleed the air out of the feed line, save having to work that air all the way through the system.
The reservoir was again topped up and the bleed nipple on the caliper cracked open, allowing the system to gravity bleed once bled cleanly, I tied the brake lever down as with the front brake, to allow a reverse bleed to the reservoir overnight - in the morning solid and no leaks!
The next logical thing to do would be to add the coolant, so suitable coolant was diluted as per the instructions. Before I added any coolant, I went round the system and made sure all the hoses were tightly secured and the drain plug was torqued up. Once I was happy, the filler cap was removed and a funnel was popped into the filler hose, allowing coolant to be poured in and the air bubble out...

... slowly 2.5L of diluted coolant was added and another batch was made up before being slowly added to the point the coolant reached the top of the filler hose and once I was happy the system was as bled as it was going to be for now, the expansion tank was topped up. This allowed the filler caps to be replaced. A check under the bike confirmed no puddles of coolant - success for now!
This concludes the mechanical commissioning of the bike - bar the first run up to temperature which will have to wait until after the tank is back on.
It's also worth saying that once that run up to temperature has occurred, I'll again check all the levels of all the fluids to ensure everything is where it needs to be.
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