With the frame ready for the yokes, it was time to get them done. The yokes were in fairly good condition but a few dings and a headstock bearing which fell apart on removal from the frame, this’ll get the works.
It’s worth nothing at this point these are marked as Showa yokes on both top and bottom yoke.
I wound the top yoke off the stem and drifted the upper headstock bearing holder out off the yoke and pushed this out until it was free with the upper headstock bearing drifted out of the holder via the 2 drift holes.
The lower bearing was drifted off the bottom yoke, using the 2 drift holes…
and that is everything disassembled.
The yokes themselves, as the largest components, were treated first. These were stripped by a wire brush attachment on a drill and masked up before being brought together with the front fork lowers and bridging piece ready for painting.
The top yoke, bottom yoke and handlebar clamps were masked up to prevent pain getting on the bearing surfaces for the forks and the handlebars, before they were treated to Autotek Etch Primer, Halfords Enamel Gloss Black and Halfords Enamel Clear Lacquer and put aside to cure.
While that was curing, the rest of the parts were inspected for corrosion …
… and cleaned up to allow reassembly…
With the headstock bearings falling apart when these were removed and therefore the bottom races removed from the headstock during the frame work, it was time to replace these ready for the yokes to go back on.
To achieve this a tool was made up from penny washers, standard washers, M8 threaded bar and a couple of nuts.
The headstock slots for the races were cleaned up and the new bottom races were pushed into the headstock and aligned by hand and measuring tool before the made up tool was added and would up to take out the slack …
… over the next hour or so, the nuts were tightened by 1/4 turn and the alignment checked, the tool repostioned, slack taken up and the tool tightened by 1/4 turn and the process continued until these were firmly in their seating slots.
The bearings and top race were then added to the bottom yoke, the new dust seal put in place before the steering stem was lightly lubricated with fork oil (because that is what I had out at the time) and the bearings and race heated up evenly with a blow torch for about 30 seconds and popped over the steering stem, and they slotted directly into place, no drifting required.
The process was repeated with the top race nut and both allowed to cool before continuing (time for a cuppa!).
Both of the bearings were then greased up with bearing grease and the lower yoke slide into the headstock and the top bearing nut applied to hold it in place. The top nut was tightened as tight as I felt appropriate (using a universal grab/super wrench to ease the job) to preload the bearings …
… before the top nut being slackened off and retightened by hand to just dial out any freeplay when rocking the bottom yoke.
The top yoke was then applied, by fitting above the top nut and using a mallet to drive the yoke onto the top bearing nut, and the fork stantions bolted into the yokes to align them ...
… before the stem bolt and locking nut were fitted and torqued up, the stantions removed and the job completed – looking good!
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