Hi guys
Working my way through a recent K75 purchase that the PO had lost interest in getting properly running. It was his fathers and was parked up in his garage 6 or 7 years ago. 50,000 miles. Symptoms are that it starts fine but once the throttle is opened it runs really rough and has no pull at all.
So I systematically went through the bike and found the Z pipe and the big 90 pipe to the airbox split. I also replaced the plugs, air filter, fuel filter, and adjusted two tight exhaust valves. Adjusted TPS switch. The PO had also replaced the fuel injectors. The compression test is good. Fuel pressure was measured using an inline meter, at 32 psi.
Still runs rubbish.
So while thinking about next logical step, I noticed that the idle stop screw was maybe 1/8 - 1/4 inch away from the stop. I removed and freed the throttle cable from the perch to eliminate binding, routing and throttle cable adjustment as the culprit.
I then looked at the "choke" cable adjustment to see if that was adjusted incorrectly. I backed the knurled knob until I could see the cable slacken. No change was detected to the idle stop "gap". Weirdly, when I engage the choke lever it has zero effect on the idle stop gap. ( the mechanism at the throttle body rotates fine)
Even screwing the idle stop out fully didn't make contact with the stop.
Anyone got an explanation or suggestion as to what to do next?